Bio:
Email: songteng-2008@163.com
宋腾(1987—),男,助理工程师;songteng-2008@163.com
由于汽化塔压差大、易发生液泛,导致200 kt/a甲醇气相脱水法制二甲醚装置无法在高负荷工况下运行。分析了汽化塔压差大的原因,并采取了相应的改造措施。改造后,汽化塔压差稳定在36~37 kPa,二甲醚装置可以在120%~130%负荷下稳定运行。
Because of high differential pressure and flooding occurring often in gasification column, the 200 kt/a gaseous methanol dehydration to dimethyl ether unit is unable to run under high load conditions. The causes of high differential pressure in gasification column are analyzed and relevant renovation measures are taken. After revamp, the pressure differential is stabilized at 36~37 kPa, dimethyl ether unit can run steadily at 120%~130% load.